Port repairs continued today. this morning...ok, around noon, I found and glued a hole in #7 and walked away to let it harden. While that was hardening I checked my notes from when I did the porting to confirm this area is really not a very critical to flow, just make it smooth so I cleaned up 12 and its done. Just now I found and glued a hole in 6.
While the 7 was hardening I took a look at the front bank TB linkages that were giving me trouble. When I originally designed everything I wasn't really thinking that I needed 2 different designs so the front bank was a last minute change and clearly suboptimal as some were hard stopping on the spring and a couple the screws were backing out while it was running.
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I found some much stiffer springs to hold the linkage against the adjusted and cut them to a size the works well. Then I repurposed the softer springs to help secure the adjusting screws....hope fully this does the trick.
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Here's the rear bank for comparison...you can see the springs are in different placed because they operate in the opposite direction.
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