Today was to be a couple firsts, it didn't work out...which is why after like 8 year of failures I've come to dead run days. The plan was to run it with the air box on which also means starting without ether. I figured I had 2-3 hours before I wanted to make noise anyway and it it now runs decent it would be nice to maybe drive and not worry about gravel in the the intake.
Step 1, the air box. When I fitted it last time I just removed the fuel return hose with a plan to relocate it at a future date....which was today. I found a fitting that would work but in the wrong color so "for now" I used it anyway, spray painted it the right color and setup the the hot air gun to speed up the drying.
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Step 2, filter boxes installed. I never really had a plan on how to secure them so "for now" they got glued and some duck tape to hold them while it dries
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Step 3 the air air ducts. The Passenger side went right on, pleasant surprise. The driver's side I decided I had been a bit too optimistic in my ability to tuck wiring out of the way so I my some additional clearance and closed the hole with duck tape "for now"
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Not bad!
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The tires are probably too close, I'll need to seal with that but it looks ok "for now".
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Time to make noise.....why isn't it starting? Ok, a little ether in the airbox and just a couple pops???....and why is the MAP reading 16kPa when it should be close to 100???....because its broken again. There was no voltage on the10V buss so I ordered a pack of 5 power supplies for $6 delivered tomorrow to use "for now".
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But something made me dig a bit more.....and there was no 5V on the 5V buss and I was seeing about 138Ohm to ground when it should be a couple kohms. I removed the old 10V power supply I was replacing and the output conditioning stuff that never worked right so I don't use...no change. The sensors are the only other things on the buss so I clipped the sensor 5V pins one by one, no change so I guess the corrosion in the board that killed the 5V to sensor 7 has spread. I made a new 5V buss with jumper wires "for now" and the board is working again other than the 10V power supply coming tomorrow.
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So tomorrow will be get the MAP working on the bench with new bits and then onto the car and it will likely be dark so next run attempt will tentatively be Tuesday. If the MAP goes quickly I may add the hood Monday night so it looks like a car that should drive.